For those of you that have tried my jerky, I thought you might like to see how I make it.
Those of you that haven't, I do send out samples when I can.
First, I start out with a good cut of meat. I don't think you can make a silk purse out of a sows ear! Like Airstreams, start with the best and hopefully, with enough hard work, you will end up with the best!
This will end up as less than one pound of jerky.
First step is to sharpen your knives. One of my other odd quirks is sharp knives. I have about six or seven different knife sharpeners. My current favorite system is called "Edge Pro". There is nothing like trying to slice raw, wiggly meat with a dull knife.
After trimming off all surface fat I slice the eye in half length wise then male 1/4 inch thick slices.
I lay them out on a baking sheet in a single layer.
I then sprinkle them with a mixture of curing agents and a homemade Cajun mixture. Then flip them over and do the other side. It then goes in the refrigerator for 24-36 hours for the cure to work. I also make other flavors.
This is a Cajun spice I made for Marc in Washington. I ship this stuff all over the US. Some has even made it up to Maryland!
The real secret to good jerky is the proper refreshments while making it. This one is for you, Marcus!
Then it goes into a dryer. I don't smoke it anymore as it is difficult to get a uniform taste. Every piece of meat absorbs smoke differently. Some tasted great, some tasted like we had a forest fire in the kitchen. I get the flavor from the spices.
A close up view. The hardest part is to dry it enough to preserve it but not so dry that it is like eating ceramic tile.
I then vacuum seal it and put on a label.
As usual, this is all done under the watchful eye of the "Boss". Believe me, if anything falls on the floor there is no 5 second rule. The boss gets any accidents, plus any trimmings.
Friday, April 10, 2009
Wednesday, April 8, 2009
Fixing Broken Glass
With the tub removed and placed in my shop I thought I would do a little work on it. I am always amazed at how many holes people can put into an airstream. I decided to start out with a clean slate and fill all the holes.
I started out by covering all of the holes with blue painters tape. Each piece of tape is at least one hole, sometimes two or three!
Then the holes were brushed with resin, fiberglass mat was placed over them and the mat was soaked with more resin.
After this cured I fliped the whole thing over and drippled resin into each hole to fill them. Each one was then sanded smooth.
The cut seen in my previous post in the bottom drain was filled with Marine Tek epoxy and sanded smooth.
I couldn't resist leaving a little souvenir for the next person that tears this trailer apart. A business card embedded in fiberglass!
Next I will move onto the sink. Meanwhile I will continue to research painting these. I don't think "Tuff as Tile" will work because the whole thing will flex during re installation and crack the coating. I am leaning toward using the flexible bumper paint Frank used in Anna.
The required Toby picture. My wife snuck into this one.
I started out by covering all of the holes with blue painters tape. Each piece of tape is at least one hole, sometimes two or three!
Then the holes were brushed with resin, fiberglass mat was placed over them and the mat was soaked with more resin.
After this cured I fliped the whole thing over and drippled resin into each hole to fill them. Each one was then sanded smooth.
The cut seen in my previous post in the bottom drain was filled with Marine Tek epoxy and sanded smooth.
I couldn't resist leaving a little souvenir for the next person that tears this trailer apart. A business card embedded in fiberglass!
Next I will move onto the sink. Meanwhile I will continue to research painting these. I don't think "Tuff as Tile" will work because the whole thing will flex during re installation and crack the coating. I am leaning toward using the flexible bumper paint Frank used in Anna.
The required Toby picture. My wife snuck into this one.
Tuesday, February 24, 2009
Continuing with the tub-shower-sink removal.
After removing all rivets and running a putty knife between the tub-shower combo and the end cap, I was able to pick it up and move it forward in the trailer. This is where I learned something else. When lifting all of this fiberglass by yourself, you can't see a damn thing. The drain for the sink is a really tight fit. In my case, it caught and broke off the drain line that I worked so hard to save. Oh well, it broke so easily that it must have become brittle over the last forty years so I will add one more thing to the list of repairs. If you are going to remove your combo, I would recommend that you cut the drain line at the same time you cut the water supply lines.
The next step is to drill out the rivets that secure the sink surround to the tub. The unit , when assembled, will not fit out the door. The faucet must be taken off and is almost impossible to get to while assembled. Besides that, my sink is really messed up and will be replaced with one I got from Scott Goranson. Thanks Scott! Here is a photo of the mysterious "Hidden Rivets". The yellow area is the back side of the tub.
This is the area behind the tub where most of you folks post pictures of rotten or missing plywood. I guess I got lucky. Moisture but solid wood.
After all of this, this is what you end up with.
The final step was to remove the end cap which is pretty straight forward. I drilled out the rivets and replaced them with "Clecos". After getting all of the rivets out I started removing the Clecos and balancing the end cap till it dropped. It then goes out the door. The final picture shows one last surprise. More farking Olympic rivets!! More water leakage. There are about 100 of these holding on the end panels. Accepted repair method my ass. Everyone of them leaks as you can see in the photos.
Next step is to drill these out and replace with bucked rivets. Then I can continue sealing up all the leaks and run new electrical. The fun just keep happening.
The next step is to drill out the rivets that secure the sink surround to the tub. The unit , when assembled, will not fit out the door. The faucet must be taken off and is almost impossible to get to while assembled. Besides that, my sink is really messed up and will be replaced with one I got from Scott Goranson. Thanks Scott! Here is a photo of the mysterious "Hidden Rivets". The yellow area is the back side of the tub.
This is the area behind the tub where most of you folks post pictures of rotten or missing plywood. I guess I got lucky. Moisture but solid wood.
After all of this, this is what you end up with.
The final step was to remove the end cap which is pretty straight forward. I drilled out the rivets and replaced them with "Clecos". After getting all of the rivets out I started removing the Clecos and balancing the end cap till it dropped. It then goes out the door. The final picture shows one last surprise. More farking Olympic rivets!! More water leakage. There are about 100 of these holding on the end panels. Accepted repair method my ass. Everyone of them leaks as you can see in the photos.
Next step is to drill these out and replace with bucked rivets. Then I can continue sealing up all the leaks and run new electrical. The fun just keep happening.
Monday, February 23, 2009
I didn't die, I just took a break.
Well the weather finally cleared up enough to get a little time to work on the trailer. I decided to finish the removal of the insides. All I had left was the toilet sink tub shower combo and the rear end cap. I had researched the tub removal and knew that there were hidden rivets but never could find much detail. So, armed with my trusty tubing cutters and a Sawzall, I went to work. The first item was to disconnect the water lines to the sink. In the 66 Safari the water lines feed the sink faucet as well as the shower wand. There is a small access hole that is so located that you can't get in to disconnect the lines so I cut them.
As you will see in the below photo, it was a good idea! I don't think there is anybody that could have snaked their hands around in there to get these lines disconnected. Keep in mind that in this photo, the open area facing you is actually riveted to the tub/shower surround. There is no access to this area until later. The only access to the connections are thru the opening at the lower left of the photo, so just cut it.
The next step was to remove the drain lines to the sink and tub. You do this with a tool that I found at the big box orange store that has an "X" on the end. It engages the X in the bottom of the drain and it unscrews. The sink was a little tight so I applied a little heat to it and loosened the sealant and it came right out. Next was the tub drain. First attempt and the X tore out and fell to the bottom of the drain.
I used the sawzall to cut the sides and an air operated grinder to get the top flange cut in half.
The tape was applied to protect the bathtub but, I ain't that good kids!
I then put a punch on the cut lines and broke that sucker in half and removed it.
Oh well, a little Bondo and it will be good as new. I have to paint it anyway! The cuts are really shallow.
I will continue this in the next post, I have to get up and get a beer.
As you will see in the below photo, it was a good idea! I don't think there is anybody that could have snaked their hands around in there to get these lines disconnected. Keep in mind that in this photo, the open area facing you is actually riveted to the tub/shower surround. There is no access to this area until later. The only access to the connections are thru the opening at the lower left of the photo, so just cut it.
The next step was to remove the drain lines to the sink and tub. You do this with a tool that I found at the big box orange store that has an "X" on the end. It engages the X in the bottom of the drain and it unscrews. The sink was a little tight so I applied a little heat to it and loosened the sealant and it came right out. Next was the tub drain. First attempt and the X tore out and fell to the bottom of the drain.
I used the sawzall to cut the sides and an air operated grinder to get the top flange cut in half.
The tape was applied to protect the bathtub but, I ain't that good kids!
I then put a punch on the cut lines and broke that sucker in half and removed it.
Oh well, a little Bondo and it will be good as new. I have to paint it anyway! The cuts are really shallow.
I will continue this in the next post, I have to get up and get a beer.
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